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A bug ?
- Diaz
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13 Feb 2014 21:26 #20242
by Diaz
Erik
A bug ? was created by Diaz
Hello every one hope all are well. I'm using. Devo8s can any one tell why my walkera 450d01 an 3 are acting up using the deviation radio ? The tail servo starts jump and jitter and then Finley it losses speed almost dies out . When I use a regular devo 8 for the same helicopters it works fine the servo do not go crazy . Has any one experience this ? If any one can shed light it would be appreciated.
Erik
Erik
Erik
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- PhracturedBlue
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14 Feb 2014 01:00 - 14 Feb 2014 01:47 #20248
by PhracturedBlue
Replied by PhracturedBlue on topic A bug ?
Are you using Deviaton, or is this with the stock firmware?
Maybe I should create a forum for stock-firmware discussions. There isn't another good place I'm aware of for such things, and we have a lot of expertise here.
Maybe I should create a forum for stock-firmware discussions. There isn't another good place I'm aware of for such things, and we have a lot of expertise here.
Last edit: 14 Feb 2014 01:47 by PhracturedBlue.
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- vlad_vy
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14 Feb 2014 03:10 #20250
by vlad_vy
Replied by vlad_vy on topic A bug ?
Probably you incorrectly set gyro gain for tail servo. Deviation use range -100% to +100%, others Tx usually use range 0 to +100%. In that case you need recalculate gyro gain to Deviation range.
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- Diaz
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14 Feb 2014 03:38 #20251
by Diaz
Erik
Replied by Diaz on topic A bug ?
Hello thank you for you're time I'm using the deviation no stock. Im also using the template that was found here in the forum. Is the one for the walkera 450d03 .. Thanks for your time. Let me know please .
Erik
Erik
Erik
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