Hi,
I'm running a modded devo 7e together with a JD 385 quadcopter and the 4.0.1 firmware.
The problem is that even when i max out the throttle I do not get enough lift power to rise from the ground.
This worked with the original remote before I harvested the BK2423 transmitter from it.
Any ideas on how to troubleshoot this?
Thanks,
Erik