Hello,
I have a problem to run WK V100D01 with the RX2613V usinng an Devo8s with Deviation 4.01
In some forums people report(but at about 2-3 years back) that they run my components well with WK2801.
My problem is, that the tail-rotor starts running at zero-Throttle and stops at about 10% throttle while the main-rotor starts movingat 8% Throttle.
has anybody an solution to keep this setup running correct?
Thanks in advance for fast response,
bmwbiker